When the engine was rebuilt I fitted a new old stock side draft carburetor trusting in the fact it would work smoothly. I experienced a problem with the car when it was first back on the road, total lack of performance and poor acceleration. I tracked this down to a sticking choke valve which was easily fixed with lubrication. However another problem with the carb was more persistent; this was a very slight fuel leakage from around the brass pipe which the fuel feed line is attached to.
General tapping in of the brass fitting made no difference and also the use of sealant gave little improvement. I resorted to removing the brass pipe from my old original carb, smearing it with Loctite and have now cured the leakage.
Originally focused on the restoration of my November 1961 built (1962 model year) Type 3 Karmann Ghia (343) I have now extended the blog to cover the ongoing ownership of my 1964 built (1965 model year) RHD type 3 Karmann Ghia (344) purchased in 1982.
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video of our 65 on the motorway
video of our 65 on the M40 taken by Paul Donovan https://m.youtube.com/watch?v=Y5pXVCcqGfA
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It is 50 years today since my Type 34 rolled off the production line at the Karmann factory. Since leaving Germany it has lived in Denma...
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Well a little trial fitting up completed, all the bumper mounts were correct as were those for the head & fog lights and indicator &...
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